Volume 36, Number 6, December 2011/January 2012
Having made hay with my good friend, Tommy, on a number of occasions and been witness to the versatility of his engine-driven NH 68 baler, I decided I needed to modify my own NH 273 baler to function similarly. The first step, due to economics, was finding an engine the right size, at the right price. I believe Tommy's Wisconsin engine is around 15 hp, so I felt I needed a little more than that since my baler is a bit larger than his. For me, the going rate on new Honda engines was just impossible In my favor, I like to peruse the classifieds and one lucky day ran across a 24 hp Honda engine advertised really cheap. I went over to look at it and liked what I saw. Fella said it came off a Zero Turn Mower. Somebody dropped it off where he worked for some minor repair and never came back for it. Says he bought it for the repair cost and after I talked him down a little, my $75 engine was on its way home. He came down because it wouldn't run unless you were pouring fuel directly into the carburetor. It turned out to be a frozen fuel shutoff solenoid. Now that I had my engine, I could begin measuring and designing an engine mount. I first had to seek advice from the folks on The Front Porch to see if anyone had already done this and had any shortcuts. To my surprise there wasn't any firsthand knowledge. Plenty had seen them but never done it themselves. A fellow Porch Participant, Jerry, e-mailed me several photos of, I believe, his neighbor's Honda powered baler. The design was very primitive, but the concept was amazingly simple. The motor was attached to a board and was slid out and clamped in place to tighten the drive belts. Armed with what I had seen on Tommy's baler and with the simple design from Jerry's photos, I was ready. The first thing to consider was the direction of the engine's counterclockwise rotation, which means the front of the motor would need to point to the rear. Next on the design consideration was which side to mount it on. I wanted it on the pickup side, but the engine's oil cooler would be up against the plunger arm cover and not get enough air flow. With that out of the way, I noticed the baler had a lot of original holes in its frame. No need to drill new ones if you can utilize the existing ones. I used a piece of cardboard, held it up to the baler and cut and shaped it into a usable pattern. I picked through my pile of scrap metal for a flat plate and a few pieces of angle iron to make the motor mount. I clamped the prototype to the baler and drilled through the existing holes. With my mount installed, I aligned the motor so as to give plenty of clearance for the baler's plunger arm cover to operate properly and aligned the end of the motor's crankshaft with the baler's flywheel. I marked and drilled the mounting holes for the motor. I had some rubber vibration dampeners from another engine project and installed those between the engine block and the mounting plate.
A quick trip to the nearest industrial/mechanical parts store got me a double V-belt pulley for the crank and a pair of 83-inch belts for around $45. After installing those around the baler and motor, it was time for some head scratching on how to engage and disengage the motor. The original NH's used a lever with an idler pulley, so that would be a logical choice for me as well. After looking at it a couple of different ways, I settled on just welding an upright piece of angle iron to the motor mount and bolting to that a piece of flat bar with an idler pulley on the end of it. Quick trip to the mower store, and I had an idler pulley for $15. I made a simple bracket for the handle to slide through with a few strategically placed holes for a linchpin to hold the pulley in and out of contact with the drive belts. Next, I made a simple angle iron battery bracket which required drilling two holes into the baler's frame.
Todd Wrightson lives in Trinity, N.C. If you wish to receive Rural Heritage in your mailbox every other month, please Subscribe. |
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PO Box 2067, Cedar Rapids IA 52406-2067
Phone: 319-362-3027 Fax: 319-362-3046 E-Mail: |
23 September 2011
December 2, 2011 last revision